An update on the Royal Scot’s motor.
I regard reinstating the clockwork mechanism as a restoration, returning the locomotive to its authentic, original condition. However, it’s also going to be a working model and I want it to work as well as possible. So whilst a ‘factory fault’ may be ‘authentic’, I will correct it if I can and certainly if remedial work will be invisible yet improve performance. By the mid-1950s, I think it is fair to say quality control at Northampton was not as good as it might have been. Standards had definitely fallen and so had sales while the range of models offered was shrinking.
As described in my post #250, when I got it, the clockwork motor was not working at all well. I initially identified the problem as misalignment of the driven axle. Which in turn I realised was due to the motor side plates being not exactly opposite each other. I concluded the misalignment was ultimately due to the bracket that supports the control rods in front of the cab and is the means of securing the rear of the motor in the locomotive body. This bracket certainly wasn’t quite square. As can be seen here, it is entirely hand-made by cutting out, drilling and bending a piece of heavy-gauge steel plate:
It perhaps says a lot about the works at Northampton, or the volume of models being made, that a part needed for every locomotive built (albeit with variations depending on the particular type) was being scratch built for each model.
After bending the bracket so that the corners were right angles (or very nearly) I reinstated it in the motor. I was able to get the motor side plates into alignment (or very nearly) and the motor then performed apparently satisfactorily on test. Problem solved, I thought. However, working on the motor over the last few days, I kept wondering if the side plates had crept back out of alignment. Fitting the rear wheels confirmed the axle was not perpendicular to the long axis of the motor. Somehow the misalignment problem had returned.
This time I think I have found the ultimate cause. The problem was due to inaccuracy in the hand-made rear bracket. The arm that goes into the motor on the rhs (looking forward) was slightly too long:
I have shortened the arm of the bracket at the top by about 1 mm using a needle file — the area ringed above. Prior to shortening, the arm of the bracket was in contact (just) with the main spring at its anchor point, wrapped around the top pillar. As the spring moved during winding/unwinding, it was pushing on the arm of the bracket, and hence pushing backwards the right-hand side plate of the motor.
This was a tiny and difficult inaccuracy to find, but was seriously reducing the performance of the motor. I am pretty sure the motor will never have been a strong puller, using too much of the energy stored in the spring to overcome internal friction due to the misalignment of gears.
So, once the repair is finished, my Royal Scot should be the best it has ever been. Like for like, a clockwork locomotive will generally not be as powerful as an electric or live-steam engine. Add in the friction of sharp curves and heavy tinplate coaches with plain bearings — a clockwork express loco will need to be as strong as it can be. I’ll try to get 46100 as close to mechanically perfect as I can for its future service as a top-link locomotive on Rivermead Central.
Martin