Finally done on the 94xx, it took longer than planned and envisaged so the backlog grows again.
I've used a new cleaner, metal work is gloriously clean but the merest hint of solder or stain turns dark grey....uggh.
One thing to watch for is the resin block, it's heavy, surprisingly heavy for resin, well I found out why the other day after washing it, it's been impregnated with steel. The outer surface is fine and smooth but when you drill it or file it and break the surface it will start to rust after washing. It's not a great issue as the main material is resin so it's only small specks but will need a wipe before paint to remove any oxidization first.
I also royally lost it with the buffers, the white metal ones were slightly shrunken so need to be bored out for the buffer stock, on top of that the spigot on the back needing turning to fit the buffer beam holes.....FAIL
Next I tried some older brass ones we had from the same pattern, one snagged in the chucked and self destructed and looking at the other three with their pitiful casting flash, nodules inside the bore and warped bases I threw them away in disgust.....FAIL.
I also had some pure 3D ones in the box which fitted just fine but I (personal choice) was reticent to have resin taking all the mechanical forces and movements. In the end I turned up adaptor spigots to fit the buffer beam and thin walled tube for the shank, fitted the tube and then slid over a cosmetic 3D print.
I've also lost a couple of rivets on the resin bunker base, mine was deformed at the bottom front edge and bulged outward so trimming back they were sadly lost.
I've fitted inside motion (Finney7 GWR 2251 set) and there were no dramas there and it all fits, the inside cranks just need securing and the axle shaft cutting out, that'll get done on strip down.
As is my normal practice, the backhead gets done whilst the body is away for paint and fitted on return, then the floor goes in to seal the cab up.
